West Ward DX Case Study

Type of Facility and Location:

  • A pharmaceutical manufacturing facility in New Jersey.

Primary Issues:

  • The mechanical system servicing the manufacturing space could no longer maintain the proper temperature and humidity levels necessary for ongoing operations.
  • Provided a system performance restoration in order to avoid a $500,000 replacement capital expense, and costs associated with a lengthy operational downtime of system replacement.

Type of System:

  • The mechanical system included a single 100 ton HEPA filtered AHU with an 8-row coil approximately 4 ft. by 8 ft.
  • The dedicated air-cooled chiller plant sat directly adjacent to the AHU and was powered by a 480-volt 3-phase bus.

Pre-cleaning Condition of System:

  • The ambient type of particulate was a fine powder.
  • The chilled water coil appeared to be visibly clear.
  • There were multiple banks of Merv 8 and Merv 12 filtration in front of the coil and a bank of HEPA downstream from the coil.
  • However, airflow testing across the coil confirmed several blockages that were greatly affecting unit performance.
  • The chiller plant itself showed heavy contamination in the condenser coils and was constantly running all four compressors with high head pressure to achieve a 41 degree chilled water output temperature.

Services Performed:

  • Both the chilled water coil inside the AHU and the bank of condenser coils for the chiller plant were cleaned with the patented Biomik Process which incorporates:
  • Multiple alternating courses of high pressure “wet steam” and Biomik Coil Cleaner.
  • A post-cleaning Biomik Protective Coil Spray is applied.

Results:

  • There was an immediate and drastic improvement in system performance and efficiency.
  • There were gains in all psychometric values of airflow, temperature, and humidity which resulted in a 26% increase in BTU output.
  • Simultaneously there was a 9% drop in chiller plant electric draw.
  • Head pressure also dropped to produce the 41-degree chilled water output.
  • The resultant water temperature was now greatly over-cooling the manufacturing space to the point of worker discomfort, and so the set point was moved to 44 degrees.
  • Each increase of one degree of the setpoint is equal to 2.5%-3% drop in energy consumption by the chiller plant.

Savings:

  • A $500,000 equipment replacement capital expenditure project was avoided.
  • Proper environmental conditions in the manufacturing space were restored, preventing losses from poor product quality through insufficient environmental conditions.
  • A 16.5%-18% energy savings on the system operation was established moving forward which equals $7,902.00 at standard NJ rates.